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热喷涂细长杆件自动化温控系统研制及其应用

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  • 1中国机械总院集团武汉材料保护研究所有限公司; 2特种表面保护材料及应用技术国家重点实验室; 3武汉船用机械有限责任公司
袁振南(1985-),工程师,主要从事热喷涂(焊)技术及装备研发,电话:18627152575,E-mail:yuanzhennan@126.com

收稿日期: 2024-04-18

  修回日期: 2024-05-13

  录用日期: 2024-05-14

  网络出版日期: 2024-11-14

Development and Application of Automatic Temperature Control System for Thermal Spraying Slender Rods

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  • (1.China Academy of Machinery Wuhan Research Institute of Materials Protection Co., Ltd., Wuhan 430030, China;2.State Key Laboratory of Special Surface Protection Materials and Application Technology, Wuhan 430030, China;3.Wuhan Marine Machinery Plant Co., Ltd., Wuhan 430080, China)
YUAN Zhennan (1985 -), Engineer, Research Focus: Thermal Spraying and PTA Technology, Tel.:18627152575, E-mail:yuanzhennan@126.com

Received date: 2024-04-18

  Revised date: 2024-05-13

  Accepted date: 2024-05-14

  Online published: 2024-11-14

摘要

为了减少热喷涂细长杆加工过程中的变形,并提高涂层质量与加工效率,基于可编程逻辑控制器(PLC)自动控制技术研制开发了针对细长杆件热喷涂自动化温控系统,实现了细长杆件喷涂过程中的温度自动化控制,采用该系统对比研究了3 种不同温度基材上等离子喷涂Al2O3-13TiO2陶瓷涂层的性能。 结果表明:当基材温度控制在100~150 ℃时,工件变形量及涂层综合性能较优。 自动化温控系统可以实现工件的连续不间断加工,与传统依靠停枪冷却的热喷涂方式相比,其生产效率提高了50%。

本文引用格式

袁振南, 张春晖, 王辉, 余斯亮, 张岩, 高名传, 陈同舟 . 热喷涂细长杆件自动化温控系统研制及其应用[J]. 材料保护, 2024 , 57(9) : 175 -179 . DOI: 10.16577/j.issn.1001-1560.2024.0215

Abstract

In order to reduce deformation during the processing of slender rods by thermal spraying and improve coating quality and processing efficiency, a temperature control system for thermal spraying of slender rods was developed based on programmable logic controller (PLC) automatic control technology, and the temperature automatic control during the spraying process of slender rods was achieved.Though the system,the performance of plasma sprayed Al2O3-13TiO2 ceramic coatings on three different temperature substrates was compared.Results showed that when the substrate temperature was controlled between 100~150 ℃, the deformation of the workpiece and the comprehensive performance of the coating were better.The automatic temperature control system could achieve continuous and uninterrupted processing of workpieces, which increased the production efficiency by 50%compared to the traditional thermal spraying method that relied on stopping the gun for cooling.
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